<feed xmlns='http://www.w3.org/2005/Atom'>
<title>linux-stable.git/drivers/usb, branch v4.4.69</title>
<subtitle>Linux kernel stable tree</subtitle>
<link rel='alternate' type='text/html' href='https://git.tavy.me/linux-stable.git/'/>
<entry>
<title>usb: hub: Do not attempt to autosuspend disconnected devices</title>
<updated>2017-05-20T12:26:59+00:00</updated>
<author>
<name>Guenter Roeck</name>
<email>linux@roeck-us.net</email>
</author>
<published>2017-03-20T21:30:50+00:00</published>
<link rel='alternate' type='text/html' href='https://git.tavy.me/linux-stable.git/commit/?id=3d3ca81d5e359593f42daf37057818ffb68a6db5'/>
<id>3d3ca81d5e359593f42daf37057818ffb68a6db5</id>
<content type='text'>
commit f5cccf49428447dfbc9edb7a04bb8fc316269781 upstream.

While running a bind/unbind stress test with the dwc3 usb driver on rk3399,
the following crash was observed.

Unable to handle kernel NULL pointer dereference at virtual address 00000218
pgd = ffffffc00165f000
[00000218] *pgd=000000000174f003, *pud=000000000174f003,
				*pmd=0000000001750003, *pte=00e8000001751713
Internal error: Oops: 96000005 [#1] PREEMPT SMP
Modules linked in: uinput uvcvideo videobuf2_vmalloc cmac
ipt_MASQUERADE nf_nat_masquerade_ipv4 iptable_nat nf_nat_ipv4 nf_nat rfcomm
xt_mark fuse bridge stp llc zram btusb btrtl btbcm btintel bluetooth
ip6table_filter mwifiex_pcie mwifiex cfg80211 cdc_ether usbnet r8152 mii joydev
snd_seq_midi snd_seq_midi_event snd_rawmidi snd_seq snd_seq_device ppp_async
ppp_generic slhc tun
CPU: 1 PID: 29814 Comm: kworker/1:1 Not tainted 4.4.52 #507
Hardware name: Google Kevin (DT)
Workqueue: pm pm_runtime_work
task: ffffffc0ac540000 ti: ffffffc0af4d4000 task.ti: ffffffc0af4d4000
PC is at autosuspend_check+0x74/0x174
LR is at autosuspend_check+0x70/0x174
...
Call trace:
[&lt;ffffffc00080dcc0&gt;] autosuspend_check+0x74/0x174
[&lt;ffffffc000810500&gt;] usb_runtime_idle+0x20/0x40
[&lt;ffffffc000785ae0&gt;] __rpm_callback+0x48/0x7c
[&lt;ffffffc000786af0&gt;] rpm_idle+0x1e8/0x498
[&lt;ffffffc000787cdc&gt;] pm_runtime_work+0x88/0xcc
[&lt;ffffffc000249bb8&gt;] process_one_work+0x390/0x6b8
[&lt;ffffffc00024abcc&gt;] worker_thread+0x480/0x610
[&lt;ffffffc000251a80&gt;] kthread+0x164/0x178
[&lt;ffffffc0002045d0&gt;] ret_from_fork+0x10/0x40

Source:

(gdb) l *0xffffffc00080dcc0
0xffffffc00080dcc0 is in autosuspend_check
(drivers/usb/core/driver.c:1778).
1773		/* We don't need to check interfaces that are
1774		 * disabled for runtime PM.  Either they are unbound
1775		 * or else their drivers don't support autosuspend
1776		 * and so they are permanently active.
1777		 */
1778		if (intf-&gt;dev.power.disable_depth)
1779			continue;
1780		if (atomic_read(&amp;intf-&gt;dev.power.usage_count) &gt; 0)
1781			return -EBUSY;
1782		w |= intf-&gt;needs_remote_wakeup;

Code analysis shows that intf is set to NULL in usb_disable_device() prior
to setting actconfig to NULL. At the same time, usb_runtime_idle() does not
lock the usb device, and neither does any of the functions in the
traceback. This means that there is no protection against a race condition
where usb_disable_device() is removing dev-&gt;actconfig-&gt;interface[] pointers
while those are being accessed from autosuspend_check().

To solve the problem, synchronize and validate device state between
autosuspend_check() and usb_disconnect().

Acked-by: Alan Stern &lt;stern@rowland.harvard.edu&gt;
Signed-off-by: Guenter Roeck &lt;linux@roeck-us.net&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</content>
<content type='xhtml'>
<div xmlns='http://www.w3.org/1999/xhtml'>
<pre>
commit f5cccf49428447dfbc9edb7a04bb8fc316269781 upstream.

While running a bind/unbind stress test with the dwc3 usb driver on rk3399,
the following crash was observed.

Unable to handle kernel NULL pointer dereference at virtual address 00000218
pgd = ffffffc00165f000
[00000218] *pgd=000000000174f003, *pud=000000000174f003,
				*pmd=0000000001750003, *pte=00e8000001751713
Internal error: Oops: 96000005 [#1] PREEMPT SMP
Modules linked in: uinput uvcvideo videobuf2_vmalloc cmac
ipt_MASQUERADE nf_nat_masquerade_ipv4 iptable_nat nf_nat_ipv4 nf_nat rfcomm
xt_mark fuse bridge stp llc zram btusb btrtl btbcm btintel bluetooth
ip6table_filter mwifiex_pcie mwifiex cfg80211 cdc_ether usbnet r8152 mii joydev
snd_seq_midi snd_seq_midi_event snd_rawmidi snd_seq snd_seq_device ppp_async
ppp_generic slhc tun
CPU: 1 PID: 29814 Comm: kworker/1:1 Not tainted 4.4.52 #507
Hardware name: Google Kevin (DT)
Workqueue: pm pm_runtime_work
task: ffffffc0ac540000 ti: ffffffc0af4d4000 task.ti: ffffffc0af4d4000
PC is at autosuspend_check+0x74/0x174
LR is at autosuspend_check+0x70/0x174
...
Call trace:
[&lt;ffffffc00080dcc0&gt;] autosuspend_check+0x74/0x174
[&lt;ffffffc000810500&gt;] usb_runtime_idle+0x20/0x40
[&lt;ffffffc000785ae0&gt;] __rpm_callback+0x48/0x7c
[&lt;ffffffc000786af0&gt;] rpm_idle+0x1e8/0x498
[&lt;ffffffc000787cdc&gt;] pm_runtime_work+0x88/0xcc
[&lt;ffffffc000249bb8&gt;] process_one_work+0x390/0x6b8
[&lt;ffffffc00024abcc&gt;] worker_thread+0x480/0x610
[&lt;ffffffc000251a80&gt;] kthread+0x164/0x178
[&lt;ffffffc0002045d0&gt;] ret_from_fork+0x10/0x40

Source:

(gdb) l *0xffffffc00080dcc0
0xffffffc00080dcc0 is in autosuspend_check
(drivers/usb/core/driver.c:1778).
1773		/* We don't need to check interfaces that are
1774		 * disabled for runtime PM.  Either they are unbound
1775		 * or else their drivers don't support autosuspend
1776		 * and so they are permanently active.
1777		 */
1778		if (intf-&gt;dev.power.disable_depth)
1779			continue;
1780		if (atomic_read(&amp;intf-&gt;dev.power.usage_count) &gt; 0)
1781			return -EBUSY;
1782		w |= intf-&gt;needs_remote_wakeup;

Code analysis shows that intf is set to NULL in usb_disable_device() prior
to setting actconfig to NULL. At the same time, usb_runtime_idle() does not
lock the usb device, and neither does any of the functions in the
traceback. This means that there is no protection against a race condition
where usb_disable_device() is removing dev-&gt;actconfig-&gt;interface[] pointers
while those are being accessed from autosuspend_check().

To solve the problem, synchronize and validate device state between
autosuspend_check() and usb_disconnect().

Acked-by: Alan Stern &lt;stern@rowland.harvard.edu&gt;
Signed-off-by: Guenter Roeck &lt;linux@roeck-us.net&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</pre>
</div>
</content>
</entry>
<entry>
<title>usb: hub: Fix error loop seen after hub communication errors</title>
<updated>2017-05-20T12:26:59+00:00</updated>
<author>
<name>Guenter Roeck</name>
<email>linux@roeck-us.net</email>
</author>
<published>2017-03-20T18:16:11+00:00</published>
<link rel='alternate' type='text/html' href='https://git.tavy.me/linux-stable.git/commit/?id=0b4dad7c2cf4139989386db0ac0cf86639692fd9'/>
<id>0b4dad7c2cf4139989386db0ac0cf86639692fd9</id>
<content type='text'>
commit 245b2eecee2aac6fdc77dcafaa73c33f9644c3c7 upstream.

While stress testing a usb controller using a bind/unbind looop, the
following error loop was observed.

usb 7-1.2: new low-speed USB device number 3 using xhci-hcd
usb 7-1.2: hub failed to enable device, error -108
usb 7-1-port2: cannot disable (err = -22)
usb 7-1-port2: couldn't allocate usb_device
usb 7-1-port2: cannot disable (err = -22)
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: activate --&gt; -22
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: activate --&gt; -22
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: activate --&gt; -22
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: activate --&gt; -22
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: activate --&gt; -22
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: activate --&gt; -22
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: activate --&gt; -22
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: activate --&gt; -22
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
** 57 printk messages dropped ** hub 7-1:1.0: activate --&gt; -22
** 82 printk messages dropped ** hub 7-1:1.0: hub_ext_port_status failed (err = -22)

This continues forever. After adding tracebacks into the code,
the call sequence leading to this is found to be as follows.

[&lt;ffffffc0007fc8e0&gt;] hub_activate+0x368/0x7b8
[&lt;ffffffc0007fceb4&gt;] hub_resume+0x2c/0x3c
[&lt;ffffffc00080b3b8&gt;] usb_resume_interface.isra.6+0x128/0x158
[&lt;ffffffc00080b5d0&gt;] usb_suspend_both+0x1e8/0x288
[&lt;ffffffc00080c9c4&gt;] usb_runtime_suspend+0x3c/0x98
[&lt;ffffffc0007820a0&gt;] __rpm_callback+0x48/0x7c
[&lt;ffffffc00078217c&gt;] rpm_callback+0xa8/0xd4
[&lt;ffffffc000786234&gt;] rpm_suspend+0x84/0x758
[&lt;ffffffc000786ca4&gt;] rpm_idle+0x2c8/0x498
[&lt;ffffffc000786ed4&gt;] __pm_runtime_idle+0x60/0xac
[&lt;ffffffc00080eba8&gt;] usb_autopm_put_interface+0x6c/0x7c
[&lt;ffffffc000803798&gt;] hub_event+0x10ac/0x12ac
[&lt;ffffffc000249bb8&gt;] process_one_work+0x390/0x6b8
[&lt;ffffffc00024abcc&gt;] worker_thread+0x480/0x610
[&lt;ffffffc000251a80&gt;] kthread+0x164/0x178
[&lt;ffffffc0002045d0&gt;] ret_from_fork+0x10/0x40

kick_hub_wq() is called from hub_activate() even after failures to
communicate with the hub. This results in an endless sequence of
hub event -&gt; hub activate -&gt; wq trigger -&gt; hub event -&gt; ...

Provide two solutions for the problem.

- Only trigger the hub event queue if communication with the hub
  is successful.
- After a suspend failure, only resume already suspended interfaces
  if the communication with the device is still possible.

Each of the changes fixes the observed problem. Use both to improve
robustness.

Acked-by: Alan Stern &lt;stern@rowland.harvard.edu&gt;
Signed-off-by: Guenter Roeck &lt;linux@roeck-us.net&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</content>
<content type='xhtml'>
<div xmlns='http://www.w3.org/1999/xhtml'>
<pre>
commit 245b2eecee2aac6fdc77dcafaa73c33f9644c3c7 upstream.

While stress testing a usb controller using a bind/unbind looop, the
following error loop was observed.

usb 7-1.2: new low-speed USB device number 3 using xhci-hcd
usb 7-1.2: hub failed to enable device, error -108
usb 7-1-port2: cannot disable (err = -22)
usb 7-1-port2: couldn't allocate usb_device
usb 7-1-port2: cannot disable (err = -22)
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: activate --&gt; -22
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: activate --&gt; -22
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: activate --&gt; -22
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: activate --&gt; -22
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: activate --&gt; -22
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: activate --&gt; -22
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: activate --&gt; -22
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: activate --&gt; -22
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
hub 7-1:1.0: hub_ext_port_status failed (err = -22)
** 57 printk messages dropped ** hub 7-1:1.0: activate --&gt; -22
** 82 printk messages dropped ** hub 7-1:1.0: hub_ext_port_status failed (err = -22)

This continues forever. After adding tracebacks into the code,
the call sequence leading to this is found to be as follows.

[&lt;ffffffc0007fc8e0&gt;] hub_activate+0x368/0x7b8
[&lt;ffffffc0007fceb4&gt;] hub_resume+0x2c/0x3c
[&lt;ffffffc00080b3b8&gt;] usb_resume_interface.isra.6+0x128/0x158
[&lt;ffffffc00080b5d0&gt;] usb_suspend_both+0x1e8/0x288
[&lt;ffffffc00080c9c4&gt;] usb_runtime_suspend+0x3c/0x98
[&lt;ffffffc0007820a0&gt;] __rpm_callback+0x48/0x7c
[&lt;ffffffc00078217c&gt;] rpm_callback+0xa8/0xd4
[&lt;ffffffc000786234&gt;] rpm_suspend+0x84/0x758
[&lt;ffffffc000786ca4&gt;] rpm_idle+0x2c8/0x498
[&lt;ffffffc000786ed4&gt;] __pm_runtime_idle+0x60/0xac
[&lt;ffffffc00080eba8&gt;] usb_autopm_put_interface+0x6c/0x7c
[&lt;ffffffc000803798&gt;] hub_event+0x10ac/0x12ac
[&lt;ffffffc000249bb8&gt;] process_one_work+0x390/0x6b8
[&lt;ffffffc00024abcc&gt;] worker_thread+0x480/0x610
[&lt;ffffffc000251a80&gt;] kthread+0x164/0x178
[&lt;ffffffc0002045d0&gt;] ret_from_fork+0x10/0x40

kick_hub_wq() is called from hub_activate() even after failures to
communicate with the hub. This results in an endless sequence of
hub event -&gt; hub activate -&gt; wq trigger -&gt; hub event -&gt; ...

Provide two solutions for the problem.

- Only trigger the hub event queue if communication with the hub
  is successful.
- After a suspend failure, only resume already suspended interfaces
  if the communication with the device is still possible.

Each of the changes fixes the observed problem. Use both to improve
robustness.

Acked-by: Alan Stern &lt;stern@rowland.harvard.edu&gt;
Signed-off-by: Guenter Roeck &lt;linux@roeck-us.net&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</pre>
</div>
</content>
</entry>
<entry>
<title>usb: misc: add missing continue in switch</title>
<updated>2017-05-20T12:26:59+00:00</updated>
<author>
<name>Gustavo A. R. Silva</name>
<email>garsilva@embeddedor.com</email>
</author>
<published>2017-04-04T03:48:40+00:00</published>
<link rel='alternate' type='text/html' href='https://git.tavy.me/linux-stable.git/commit/?id=6c3785cca656284d6ccd7bd098d7516bb320da64'/>
<id>6c3785cca656284d6ccd7bd098d7516bb320da64</id>
<content type='text'>
commit 2c930e3d0aed1505e86e0928d323df5027817740 upstream.

Add missing continue in switch.

Addresses-Coverity-ID: 1248733
Signed-off-by: Gustavo A. R. Silva &lt;garsilva@embeddedor.com&gt;
Acked-by: Alan Stern &lt;stern@rowland.harvard.edu&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</content>
<content type='xhtml'>
<div xmlns='http://www.w3.org/1999/xhtml'>
<pre>
commit 2c930e3d0aed1505e86e0928d323df5027817740 upstream.

Add missing continue in switch.

Addresses-Coverity-ID: 1248733
Signed-off-by: Gustavo A. R. Silva &lt;garsilva@embeddedor.com&gt;
Acked-by: Alan Stern &lt;stern@rowland.harvard.edu&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</pre>
</div>
</content>
</entry>
<entry>
<title>USB: Proper handling of Race Condition when two USB class drivers try to call init_usb_class simultaneously</title>
<updated>2017-05-20T12:26:58+00:00</updated>
<author>
<name>Ajay Kaher</name>
<email>ajay.kaher@samsung.com</email>
</author>
<published>2017-03-28T12:09:32+00:00</published>
<link rel='alternate' type='text/html' href='https://git.tavy.me/linux-stable.git/commit/?id=de9d2d297ebe4d591efd41902c568e3ef4774c43'/>
<id>de9d2d297ebe4d591efd41902c568e3ef4774c43</id>
<content type='text'>
commit 2f86a96be0ccb1302b7eee7855dbee5ce4dc5dfb upstream.

There is race condition when two USB class drivers try to call
init_usb_class at the same time and leads to crash.
code path: probe-&gt;usb_register_dev-&gt;init_usb_class

To solve this, mutex locking has been added in init_usb_class() and
destroy_usb_class().

As pointed by Alan, removed "if (usb_class)" test from destroy_usb_class()
because usb_class can never be NULL there.

Signed-off-by: Ajay Kaher &lt;ajay.kaher@samsung.com&gt;
Acked-by: Alan Stern &lt;stern@rowland.harvard.edu&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</content>
<content type='xhtml'>
<div xmlns='http://www.w3.org/1999/xhtml'>
<pre>
commit 2f86a96be0ccb1302b7eee7855dbee5ce4dc5dfb upstream.

There is race condition when two USB class drivers try to call
init_usb_class at the same time and leads to crash.
code path: probe-&gt;usb_register_dev-&gt;init_usb_class

To solve this, mutex locking has been added in init_usb_class() and
destroy_usb_class().

As pointed by Alan, removed "if (usb_class)" test from destroy_usb_class()
because usb_class can never be NULL there.

Signed-off-by: Ajay Kaher &lt;ajay.kaher@samsung.com&gt;
Acked-by: Alan Stern &lt;stern@rowland.harvard.edu&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</pre>
</div>
</content>
</entry>
<entry>
<title>USB: serial: ftdi_sio: add device ID for Microsemi/Arrow SF2PLUS Dev Kit</title>
<updated>2017-05-20T12:26:58+00:00</updated>
<author>
<name>Marek Vasut</name>
<email>marex@denx.de</email>
</author>
<published>2017-04-18T18:07:56+00:00</published>
<link rel='alternate' type='text/html' href='https://git.tavy.me/linux-stable.git/commit/?id=fcd9a083cd2283574c46b78f39f0d7a83c3cc7d6'/>
<id>fcd9a083cd2283574c46b78f39f0d7a83c3cc7d6</id>
<content type='text'>
commit 31c5d1922b90ddc1da6a6ddecef7cd31f17aa32b upstream.

This development kit has an FT4232 on it with a custom USB VID/PID.
The FT4232 provides four UARTs, but only two are used. The UART 0
is used by the FlashPro5 programmer and UART 2 is connected to the
SmartFusion2 CortexM3 SoC UART port.

Note that the USB VID is registered to Actel according to Linux USB
VID database, but that was acquired by Microsemi.

Signed-off-by: Marek Vasut &lt;marex@denx.de&gt;
Signed-off-by: Johan Hovold &lt;johan@kernel.org&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</content>
<content type='xhtml'>
<div xmlns='http://www.w3.org/1999/xhtml'>
<pre>
commit 31c5d1922b90ddc1da6a6ddecef7cd31f17aa32b upstream.

This development kit has an FT4232 on it with a custom USB VID/PID.
The FT4232 provides four UARTs, but only two are used. The UART 0
is used by the FlashPro5 programmer and UART 2 is connected to the
SmartFusion2 CortexM3 SoC UART port.

Note that the USB VID is registered to Actel according to Linux USB
VID database, but that was acquired by Microsemi.

Signed-off-by: Marek Vasut &lt;marex@denx.de&gt;
Signed-off-by: Johan Hovold &lt;johan@kernel.org&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</pre>
</div>
</content>
</entry>
<entry>
<title>usb: host: xhci: print correct command ring address</title>
<updated>2017-05-20T12:26:58+00:00</updated>
<author>
<name>Peter Chen</name>
<email>peter.chen@nxp.com</email>
</author>
<published>2017-04-19T13:55:52+00:00</published>
<link rel='alternate' type='text/html' href='https://git.tavy.me/linux-stable.git/commit/?id=af3c8bf0e06b73039a64071565e06805d0adbc3c'/>
<id>af3c8bf0e06b73039a64071565e06805d0adbc3c</id>
<content type='text'>
commit 6fc091fb0459ade939a795bfdcaf645385b951d4 upstream.

Print correct command ring address using 'val_64'.

Signed-off-by: Peter Chen &lt;peter.chen@nxp.com&gt;
Signed-off-by: Mathias Nyman &lt;mathias.nyman@linux.intel.com&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</content>
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<pre>
commit 6fc091fb0459ade939a795bfdcaf645385b951d4 upstream.

Print correct command ring address using 'val_64'.

Signed-off-by: Peter Chen &lt;peter.chen@nxp.com&gt;
Signed-off-by: Mathias Nyman &lt;mathias.nyman@linux.intel.com&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</pre>
</div>
</content>
</entry>
<entry>
<title>USB: serial: io_edgeport: fix descriptor error handling</title>
<updated>2017-05-14T11:32:57+00:00</updated>
<author>
<name>Johan Hovold</name>
<email>johan@kernel.org</email>
</author>
<published>2017-01-12T13:56:14+00:00</published>
<link rel='alternate' type='text/html' href='https://git.tavy.me/linux-stable.git/commit/?id=7bb6405d93ff5cfc35ad4f735a96141107ab22b0'/>
<id>7bb6405d93ff5cfc35ad4f735a96141107ab22b0</id>
<content type='text'>
commit 3c0e25d883d06a1fbd1ad35257e8abaa57befb37 upstream.

Make sure to detect short control-message transfers and log an error
when reading incomplete manufacturer and boot descriptors.

Note that the default all-zero descriptors will now be used after a
short transfer is detected instead of partially initialised ones.

Fixes: 1da177e4c3f4 ("Linux-2.6.12-rc2")
Reviewed-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;
Signed-off-by: Johan Hovold &lt;johan@kernel.org&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

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commit 3c0e25d883d06a1fbd1ad35257e8abaa57befb37 upstream.

Make sure to detect short control-message transfers and log an error
when reading incomplete manufacturer and boot descriptors.

Note that the default all-zero descriptors will now be used after a
short transfer is detected instead of partially initialised ones.

Fixes: 1da177e4c3f4 ("Linux-2.6.12-rc2")
Reviewed-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;
Signed-off-by: Johan Hovold &lt;johan@kernel.org&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</pre>
</div>
</content>
</entry>
<entry>
<title>USB: serial: mct_u232: fix modem-status error handling</title>
<updated>2017-05-14T11:32:57+00:00</updated>
<author>
<name>Johan Hovold</name>
<email>johan@kernel.org</email>
</author>
<published>2017-01-12T13:56:16+00:00</published>
<link rel='alternate' type='text/html' href='https://git.tavy.me/linux-stable.git/commit/?id=574c8b2aa05f8ce5cd5e170016943ed3505c750e'/>
<id>574c8b2aa05f8ce5cd5e170016943ed3505c750e</id>
<content type='text'>
commit 36356a669eddb32917fc4b5c2b9b8bf80ede69de upstream.

Make sure to detect short control-message transfers so that errors are
logged when reading the modem status at open.

Note that while this also avoids initialising the modem status using
uninitialised heap data, these bits could not leak to user space as they
are currently not used.

Fixes: 1da177e4c3f4 ("Linux-2.6.12-rc2")
Reviewed-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;
Signed-off-by: Johan Hovold &lt;johan@kernel.org&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

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commit 36356a669eddb32917fc4b5c2b9b8bf80ede69de upstream.

Make sure to detect short control-message transfers so that errors are
logged when reading the modem status at open.

Note that while this also avoids initialising the modem status using
uninitialised heap data, these bits could not leak to user space as they
are currently not used.

Fixes: 1da177e4c3f4 ("Linux-2.6.12-rc2")
Reviewed-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;
Signed-off-by: Johan Hovold &lt;johan@kernel.org&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</pre>
</div>
</content>
</entry>
<entry>
<title>USB: serial: quatech2: fix control-message error handling</title>
<updated>2017-05-14T11:32:57+00:00</updated>
<author>
<name>Johan Hovold</name>
<email>johan@kernel.org</email>
</author>
<published>2017-01-12T13:56:20+00:00</published>
<link rel='alternate' type='text/html' href='https://git.tavy.me/linux-stable.git/commit/?id=ea04bd7914995c660c4f5504929b4a8bdced99fe'/>
<id>ea04bd7914995c660c4f5504929b4a8bdced99fe</id>
<content type='text'>
commit 8c34cb8ddfe808d557b51da983ff10c02793beb2 upstream.

Make sure to detect short control-message transfers when fetching
modem and line state in open and when retrieving registers.

This specifically makes sure that an errno is returned to user space on
errors in TIOCMGET instead of a zero bitmask.

Also drop the unused getdevice function which also lacked appropriate
error handling.

Fixes: f7a33e608d9a ("USB: serial: add quatech2 usb to serial driver")
Reviewed-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;
Signed-off-by: Johan Hovold &lt;johan@kernel.org&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</content>
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<pre>
commit 8c34cb8ddfe808d557b51da983ff10c02793beb2 upstream.

Make sure to detect short control-message transfers when fetching
modem and line state in open and when retrieving registers.

This specifically makes sure that an errno is returned to user space on
errors in TIOCMGET instead of a zero bitmask.

Also drop the unused getdevice function which also lacked appropriate
error handling.

Fixes: f7a33e608d9a ("USB: serial: add quatech2 usb to serial driver")
Reviewed-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;
Signed-off-by: Johan Hovold &lt;johan@kernel.org&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</pre>
</div>
</content>
</entry>
<entry>
<title>USB: serial: ftdi_sio: fix latency-timer error handling</title>
<updated>2017-05-14T11:32:56+00:00</updated>
<author>
<name>Johan Hovold</name>
<email>johan@kernel.org</email>
</author>
<published>2017-01-12T13:56:12+00:00</published>
<link rel='alternate' type='text/html' href='https://git.tavy.me/linux-stable.git/commit/?id=f15ca928dc2a5118f1dead4060b6fa2c4e5b1576'/>
<id>f15ca928dc2a5118f1dead4060b6fa2c4e5b1576</id>
<content type='text'>
commit e3e574ad85a208cb179f33720bb5f12b453de33c upstream.

Make sure to detect short responses when reading the latency timer to
avoid using stale buffer data.

Note that no heap data would currently leak through sysfs as
ASYNC_LOW_LATENCY is set by default.

Fixes: 1da177e4c3f4 ("Linux-2.6.12-rc2")
Reviewed-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;
Signed-off-by: Johan Hovold &lt;johan@kernel.org&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</content>
<content type='xhtml'>
<div xmlns='http://www.w3.org/1999/xhtml'>
<pre>
commit e3e574ad85a208cb179f33720bb5f12b453de33c upstream.

Make sure to detect short responses when reading the latency timer to
avoid using stale buffer data.

Note that no heap data would currently leak through sysfs as
ASYNC_LOW_LATENCY is set by default.

Fixes: 1da177e4c3f4 ("Linux-2.6.12-rc2")
Reviewed-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;
Signed-off-by: Johan Hovold &lt;johan@kernel.org&gt;
Signed-off-by: Greg Kroah-Hartman &lt;gregkh@linuxfoundation.org&gt;

</pre>
</div>
</content>
</entry>
</feed>
